Ok I just got home from the 4 hour drive.
So on the idle tensioner pulley the bolt that pretty much holds it in place was the wrong bolt size so that caused the belt & pulley at high rpms to wiggle and move abit on the SC pulley. The belt started to tear on the sides and come apart. Tommy found that problem right away so new bolt and new belt is on the way.
At 24psi and 13 degrees of timing we made 968rwhp and 958 torque with very little timing. Tim and Tommy we’re just getting started with their secret sauce.
With the ice box iat’s we’re at 106 and cooling temp was at 58 degrees. I’m thinking at 18-20 degrees of timing we will see 1050rwhp plus. Man that ice box makes a huge difference. After each pull I could literally put my hand on the Magnuson and it never got hot. Maybe Friday this week back on the dyno or next week. The highest rpm level we took it to on the dyno was at 6100rpm. A lot more room to make power. If you look close on the SC pulley belt moved over 1 rib and idle tensioner moved a bit to as well.
On the positive note no belt slippage this time.
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